1. Mwambao wa Ajali
1.1 Muundo na Uhusiano wa Transformer wa Umeme wa GIS wa 35kV
ZX2 ya gas-insulated double-bus switchgear, iliyotengenezwa mnamo Machi 2011 na iliyorudi kazi rasmi mnamo Julai 2012, imeundwa na viwanja vya bus voltage transformers (PTs) vya mbili kwa kila sehemu ya bus. Viwanja vya PT vya sehemu moja ya bus vilivyovunjika vimeundwa katika mfuko mmoja wa switchgear una upana wa 600 mm. PTs za tatu zimeelekezwa kama muundo wa penzi chini ya mfuko.
PTs zimeunganishwa na disconnectors katika chumba cha bus cha PT switchgear kupitia cables ngumu nyingi. Disconnectors zimeunganishwa na bus tatu kupitia moving contacts katika SF₆ fully-enclosed bus chamber. Muundo mzima wa bus unapunguza kiwango cha matatizo, na bus haijafikia na bus protection maalum. Matatizo ya bus yanatathmini kwa njia ya backup protection ya power incoming switch.
1.2 Nyanja ya Kazi Kabla ya Kubakisha
Kabla ya ajali, grid ya umeme ilifanya kazi kama ifuatavyo:
Mfumo wa 220kV: Qiaoshi Line na Huishi Line zilikuwa zinazozingatia kwa bus tie switch iliyofungwa.
Mchuzi wa Main Transformer: No.1 main transformer alikuwa na 47 MW, na No.2 alikuwa na 14 MW.
Mfumo wa 35kV: Unit A ilikuwa inafanya kazi na double buses kwa split operation. Generator No.2, anayezingatia 30.5 MW, ilikuwa imeunganishwa na Bus II ya Unit A kupitia Bus 1 ya Unit E, hot oil interconnection line switchgears 361 na 367, na ilikuwa inafanya kazi kwa pamoja na No.2 main transformer.
1.3 Mzunguko wa Ajali
Unganisho wa Matatizo
Tangu saa 15:11:20.393 tarehe 19 April, kifaa cha protection cha switch 367 katika Unit E (Bus Unit for Generators 1 and 2) kilipewa mara kwa mara PT disconnection alarms, ambayo zilikuwa zinachukua muda kwa muda.
Kubakisha Vifaa
Utambuzi wa Mtaani
Lango la mfuko lilikuwa limelianguliwa. Phase A PT ilikuwa imebakishwa sana, na plug ya Phase B ilikuwa imeshindwa. Vifaa vya ndani vilikuwa vimechomoka.
Secondary wires za mfuko wa arrester wa karibu walikuwa wameharibika. Chambani ya bus pressure na insulation tests zilikuwa safi.
2. Tathmini ya Sababu
2.1 Ubora wa Vifaa na Matatizo ya Upatikanaji
2.2 Nyanja Zisizotumaini
2.3 Tathmini ya Manufacturer's Disassembly
Eneo la Matatizo
Tathmini ya Stress
Cable connections isiyotumaini yalitokana na transverse stress concentrated at flange holes.
Fault progression: Intermittent grounding → Aluminum coating ablation → Fault reset → Final breakdown.

3. Mpango wa Kutenganisha
3.1 Usimamizi wa Monitoring wa Vifaa
3.2 Maendeleo ya Structural Design
Cabinet Expansion: Increase cabinet width kutoka 600 mm hadi 800 mm ili kutumainisha heat dissipation.
Connection Upgrade: Replace short cable plugs na direct connections ili kurudisha stress.
Modular Design: Adopt pluggable PTs/arresters ili kukurudisha muda wa huduma.
3.3 Enhancement ya Protection System
Add dedicated circuit breakers kwa PT switchgears na overcurrent/overvoltage protection.
Install dedicated bus protection devices kwa rapid fault isolation.
Optimize zero-sequence circuit design ili kurudisha resonance risk.
3.4 Strategy Adjustment ya Operation and Maintenance
Establish full lifecycle management records kwa vifaa, kudokumenta installation na maintenance data.
Perform quarterly SF₆ moisture content tests na threshold ≤300 ppm.
Conduct annual PT volt-ampere characteristic tests kwa comparison na factory data.
4. Lessons Learned and Preventive Measures
4.1 Key Lessons
Design Flaw: Co-location of PTs increased fault propagation risk.
Maintenance Gap: Failure to detect cumulative stress damage.
Protection Deficiency: Reliance on backup protection delayed fault clearance.
4.2 Preventive Measures
Strengthen equipment manufacturing supervision, focusing on insulation processes and structural integrity.
Promote condition-based maintenance using vibration monitoring to assess stress levels.
Revise design specifications to mandate flexible connections between PTs and buses.
Conduct anti-accident drills to standardize emergency response procedures for PT faults.
4.3 Implementation Results
Post-retrofit data shows:
Partial discharge reduced from 80 pC to 15 pC.
Temperature rise under full load decreased by 12°C.
Fault response time shortened from 600 ms to 40 ms.
5. Conclusion
This accident revealed multiple hidden risks in GIS equipment design, installation, and maintenance. Through structural optimization, protection system upgrade, and management enhancement, a comprehensive risk prevention system has been established. Continuous monitoring of equipment performance will provide replicable retrofit experience for similar substations.